Technology in Action
Setting a critical well barrier in tubing with damaged nipple profiles.
Collection of data with minimal pressure loss in flowing wells.
Contingency barrier option on high value subsea wells to avoid additional rig costs.
Recovery of magnetic junk in high temperature wells.
Hard scale removal at multiple obstruction points.
Retrieval of equipment lost in the well and fast-track production restart.
High Deviation Heavy Duty Fishing in North Sea.
Recovery of Safety Valve Lockout Tool which had parted downhole.
Retrieval of Sub-Surface Safety Valve (SSSV) with damaged Fish Neck.
Retrieval of Injection Valve backed off from 7” Retrievable Bridge Plug (RBP).
Trial deployment of slickline set SIM plugs and Peak Latch/Seal micro coil stinger for the purpose of selective zonal isolation and treatment.
Data acquisition to monitor pressure build-up in a shut-in well.
Design a new tool that ensures the successful release of Tubing Conveyed Perforating (TCP) Guns from the suspension system in highly deviated wells, t…
Evaluation of an e-line deployed well tractor, well stroker, and slickline configuration toolstring for mechanical well interventions in highly deviat…
To conduct a trial test to remove hard scale from production tubing using mechanical means thus restoring full bore access.
To cut 0.125” OD GD31MO wire at rope socket to enable the retrieval of stuck toolstring.
Retrieval of injection valve from tubing crossover at 10,400ft.
High deviation fishing at depth in the Middle East.
Isolation of failed inflow valve at high deviation.
Successful location and stabilisation of a leak path in the completion string.
Full workover avoided through innovative use of an LWIV to perform first subsea slickline intervention in Nigeria.
Efficient straddle solution enables successful repair of production X-tree.