Setting a critical well barrier in tubing with damaged nipple profiles Collection of data with minimal pressure loss in flowing wells Contingency barrier option on high-value subsea wells > Recovery of magnetic junk in high temperature wells Hard scale removal at multiple obstruction points Retrieval of equipment lost in the well and fast-track production restart High deviation, heavy-duty fishing, North Sea Recovery of safety valve lockout tool which had parted downhole Retrieval of sub-surface safety valve (SSSV) with damaged fish neck Retrieval of injection valve backed off from 7-in retrievable bridge plug Trial deployment of slickline-set SIM plugs and Peak latch/seal micro coil stinger Data acquisition to monitor pressure buildup in a shut-in well Bespoke activation tool design Evaluation of an e-line deployed tractor, stroker, and slickline toolstring Trial test to remove hard scale from production tubing using mechanical means Cut wire at rope socket to retrieve stuck toolstring Retrieval of injection valve from tubing crossover at 10,400 ft High-deviation fishing at depth in the Middle East Isolation of failed inflow valve at high deviation Location and stabilization of a leak path in the completion string Innovative use of an LWIV to perform first subsea slickline intervention in Nigeria Efficient straddle solution enables repair of production Christmas tree Permanent plug keeps P&A project moving Peak eCutter facilitates faster stuck toolstring recovery in long-reach, highly-deviated well Retrievable sand screen anchoring system eliminates leaks Mechanical scale removal saves USD 250,000 PTTEP gas lift straddle conversion restores oil production for mature well Slickline-deployed plug isolates damage to avoid workover KOC restores oil production to 800 bbl/d using digital-slickline-conveyed straddle system D-Set setting tool and DSL digital slickline cable set large-bore gauge hanger in monobore well Retrievable bridge plug enables proper tubing cut and saves 4 rig days, Congo Remote Intervention Operation Enables Effective Planning of Plug and Abandonment Campaign Shell Removes 900-ft Parted Wireline from North Sea Well

Recovery of magnetic junk in high temperature wells

 

Technical Challenge:

Recovery of magnetic junk in high temperature wells

Peak Solution:

High temperature/high strength magnet

Customer:

OMV, New Zealand

Well Type:

1200 ft true depth, 82 degree deviation well, Maari field, New Zealand

The Challenge:

The customer was completing a workover on a well when three control line/ESP cable clamps broke free whilst retrieving the completion back to surface.

Considerations:

  • The clamps were lost in 10 ¾-in casing with 82 degree deviation
  • The well fluid contained approximately 3 percent KCl, however the Peak magnet is highly resistant to CO2 and H2S environments.

Summary:

Using a Peak 2.72-in OD high temperature/high strength magnet, the service company working on the well at the time managed to recover the clamp pieces in five tractor runs on e-line and, due to the powerful strength of the Peak magnet, even retrieved two blocks and allen key bolts lost from an earlier clamp.

Value to Customer:

Compared to other magnets available on the market, Peak’s high temperature/high strength magnet is particularly strong and can withstand prolonged exposure to very high downhole temperatures (500 degF) without losing magnetic strength. Peak’s magnet is available in a range of sizes (1.75 in up to 4.5-in OD) to suit the application and well geometry.

 

Product Code: 115